Search found 8 matches
- Sat Feb 10, 2018 3:41 am
- Forum: Developer Discussions
- Topic: Changing NRF_FLOW_CTRL pin(P0_14) found not pulse
- Replies: 2
- Views: 2101
Re: Changing NRF_FLOW_CTRL pin(P0_14) found not pulse
Thank you for your answer. I think I get it.
- Sat Feb 10, 2018 3:36 am
- Forum: Autonomous flight
- Topic: The newest TDOA2 will often have a sudden crash
- Replies: 7
- Views: 4394
Re: The newest TDOA2 will often have a sudden crash
Hi,
I also observed sudden physical crash while the Crazyflie moving slowly. I was confused about this.And when I repaired it and it can also perform well. I couldn't dope out any solution about this problem.
I also observed sudden physical crash while the Crazyflie moving slowly. I was confused about this.And when I repaired it and it can also perform well. I couldn't dope out any solution about this problem.
- Mon Feb 05, 2018 7:14 am
- Forum: Developer Discussions
- Topic: Changing NRF_FLOW_CTRL pin(P0_14) found not pulse
- Replies: 2
- Views: 2101
Changing NRF_FLOW_CTRL pin(P0_14) found not pulse
Hi, I have changed NRF_FLOW_CTRL pin(nrf51822 is P0_14 pin and stm32F4 is PA4) to new connection(nrf51822 is P0_08 pin and stm32F4 is PC15) in my own PCB. I also changed the pin init of NRF_FLOW_CTRL in stm32 and NRF firmware. I think is ok but the pulse of NRF_FLOW_CTRL pin when connected to the cl...
- Mon Feb 05, 2018 6:24 am
- Forum: Autonomous flight
- Topic: The newest TDOA2 will often have a sudden crash
- Replies: 7
- Views: 4394
Re: The newest TDOA2 will often have a sudden crash
Thank you for your help.I observed a real physical crash.I setup my system in a rectangle and fly inside the convex hull. I think it can be my quadcopters' physical problem. Now I try to repair them.Do you have some suggestion to test a quadcopter is enough stable to fly ? It often performed very we...
- Thu Feb 01, 2018 3:37 am
- Forum: Autonomous flight
- Topic: The newest TDOA2 will often have a sudden crash
- Replies: 7
- Views: 4394
Re: The newest TDOA2 will often have a sudden crash
Thank you for your answer. I have try the latest master branch of the firmware but it also happened when I control to flight in a circle.Maybe my Quadcopters are not stable enough or the position estimation of kalman filter isn't faster enough to run a quickly circle.
- Thu Feb 01, 2018 3:28 am
- Forum: Loco Positioning System
- Topic: The height of new TDOA2 is inconsistent
- Replies: 3
- Views: 2164
Re: The height of new TDOA2 is inconsistent
Hi! Thank you for your answer.I have traced the Quadcopter and get the position from the python script, the data is right which close to setposition. But I measured the height is inconsistent so much.I find this inconsistent when I using TDOA and TWR , and I find the inconsistent of height is larger...
- Wed Jan 10, 2018 6:20 am
- Forum: Autonomous flight
- Topic: The newest TDOA2 will often have a sudden crash
- Replies: 7
- Views: 4394
The newest TDOA2 will often have a sudden crash
Hi ,I find the latest version TDOA2 will often appear sudden impact crash, I'm not sure whether it is my Quadcopters' problem or others, but I have test 10 Quadcopters and found crash more easily than TWR, I don't know what cause it ? Maybe the firmware have influence on it ? can you give me some he...
- Wed Jan 10, 2018 5:56 am
- Forum: Loco Positioning System
- Topic: The height of new TDOA2 is inconsistent
- Replies: 3
- Views: 2164
The height of new TDOA2 is inconsistent
Hi,I find the height of the latest version of TDOA2 is inconsistent on the space, I set up eight anchor point in the space, a rectangle of 3.6 X 3.6 X 2.65 m, I found that the greater X axis the height is lower;the greater the Y axis, the lower the height.The difference is lager to 30 cm. How can I ...